John
Deere 317
- page 2
While I was installing the new key switch and looking at the electrical
system behind the operator's
tower, I noticed something that I had never seen before. I had
noticed that the ammeter needle didn't seem to do much but swing back
and forth with the vibrations of the tractor. When I was in
looking at the ignition switch, I noticed that there were no electrical
connections on the ammeter. This struck me a bit odd.
Normally there are at least two - current in and current out - usually
the wires come from the alternator/ regulator and proceed to the
battery. On a car, they usually have a bulb to illuminate them as
well. This one had none. I knew I would have the whole
tractor apart soon, so I made a mental note to investigate why this was
and how it worked with no connections to the charging circuit.
I got the deck back together and leveled it to the best of my ability
given what I knew of how it worked. I was still a bit fuzzy on
that part. I took her out for another test mow. Much better, but
still not quite good enough. However it was as good as it was
going to get with my present knowledge. I have to say that
compared to what I was used to, this
tractor is a beast. It is very heavy duty compared to the 130 and
the 130 puts the MTD made home center tractors to shame. I have
some cast concrete catch basins for the gutter downspouts that have
been stationary for the 20 years I've lived here. I usually edge
around them with the string trimmer, then mow up to them. I've
run into them countless times with walk behind mowers and the 130 at
low speeds. They've never budged. I got a little too close
with the 317 and pushed it a half foot before I could remember to
throttle back rather than use the brakes. The contact barely
scratched the paint on the deck. The deck is so thick that it
didn't
even flex. I'll have to be more careful. One wrong move and
I could bowl over my young cherry trees.
I started thinking about retro-fitting a 318 power steering to the
317. In the mean time, I wanted to see if I could lessen the slop
in the manual steering gear. Removing the steering gear would
give me the chance to do some measuring to see how the 318 steering
control would fit. The reading I had done on the swap seemed to
indicate that the bracket that held the manual worm and sector steering
gear was a little too close to the center line of the tractor to be
able to get the power steering controller and shaft to sit perfectly
vertical. I needed to see for myself.
Manual
steering
gear
with
right
side
up
Left
side
with
attached
arm
and
a
little
body
rust
I pulled out the battery, removed the battery pan and took a look at
the steering gear. It is an interesting setup. There are a
few more parts than are found in the usual automotive set up. The
outline is as follows: When the steering wheel is turned, the
steering shaft turns a worm gear which then turns an arm
on the side of the steering box which moves in an arc. There is a
bolt
on the end of the arm that connects to a flat bar through a hole with a
bushing in the end of the bar. This bar connects to an arm on a
shaft that runs about half the width of the tractor's frame. The
bar swivels in bushings on the right side and extends through the frame
on the left side to a clamp on steering arm. The steering arm on
the left outside of the frame attaches to a drag link which attaches to
the spindle with another clamp-on steering arm. The two spindles
are connected to each other by a tie rod with ball joints.
I don't know how many hours are on the 317, but I would guess over
1000. It appears that the previous owners didn't do much in the
way of steering maintenance as the bushings between the steering gear
and rock shaft were dry. Not only were the bushings worn out, but the
hole in the arm was worn enough that the bushings flopped around a
bit. Both bushings on the steering rock shaft were worn and the
steering gear itself was way out of adjustment.
I spent close to a half hour trying to get two of the three bolts out
that hold the steering gear to the frame. In retrospect, it would
have been easier to pull the rear sheet metal off and then remove the
operator's tower to give better access to the bolts. From the
position I was attacking the bolts, it took an offset open end wrench
and another 45°/60° combination open end wrench to turn the
bolts one flat at a time. Once I got the steering gear loose, it
was a struggle to remove the gear and steering shaft out of the
tractor. Again, removing the sheet metal would have sped up the
process.
With the gear out, I stripped it down, cleaned all parts in the solvent
tank, greased the bearings, worm gear and shaft, then reassembled
it. The adjustment procedure involves first tightening the end
cap (adjusting plug) to 10 - 14 foot pounds and securing the plug with
a cotter pin. The steering wheel is then attached and turned lock
to lock. Mine turned 3 revolutions. Split the turns in half to find the
center point. This was a turn and a half for mine. The gear
adjustments are made with the steering gear centered half way between
the locks. You are looking for a slight drag at this position and no
drag on either side of center. You then put a 0.10" feeler gauge
or spacer between the steering arm and the steering shaft and snug the
nut on the opposite side of the steering arm until the feeler is just
able to be moved. Torque the nut to 40 foot pounds and remove the
feeler. Last of all, tighten the stud and nut on the steering arm side
to 40 foot pounds. Check to see that there is a slight drag in the
centered position. Once you're done with this the steering wheel
comes back off and you can install the steering gear assembly into the
tractor.
I made up some bushings on the lathe that fit a little tighter than the
existing ones that connect the steering arm to the rock shaft. I
decided not to replace the rock shaft bushings as I was just going to
pull this all back apart soon and the rock shaft would not be used with
the power steering, so I put her all back together. The steering
was now quite acceptable with only about 8 to 10 degrees of slop.
It did absolutely nothing for the amount of force it takes to turn the
wheel with the tractor standing still. I did read an interesting
post about adding needle bearings to the bottom of each of the spindle
shafts to lessen the friction when turning the wheels, but I don't
think that this will be necessary with the addition of power steering.
While working on the steering, I took some time to take some
measurements. The 3/16" steel upright that holds the manual
steering gear is a little less than 1.25" from the center line of the
steering shaft that connects to the steering wheel. I'd need this
information to help me design a bracket to hold the 318 power steering
control valve. Speaking of which, I found a 318 steering
controller on Ebay and won it. A
five port model which I understand
to be the preferable way to go. I've read that the early 318s
came with a four port control. One port takes fluid pressure in, one
port returns fluid to the hydro and one each for pushing the steering
ram in and out to turn the wheels left and right. As I understand
it, the four port steering is plumbed in parallel with the spool valve
that operates the lift or auxiliary components and they tended to
loose power steering when the lift was operating. The five port
control has an auxiliary port that passes hydraulic pressure from the
steering control to the spool valve which allows the power steering to
operate even when using the lift.
So I had a steering controller coming. It was time to make a
decision on a steering ram. I had read that a few guys had used
the 318 ram, but hooking up the ram to the spindle arm was a bit of a
chore. I happened to be searching Ebay for steering components
and
came across a steering ram for a newer 345 model. It looked
perfect for my application. The end that attached to the spindle
arm had the same ball joint as the current drag link and the end that
mounted to the frame had a large swivel with a conical stand-off.
No one else even bid on it. Two down. I found a set of 5
port steering hydraulic lines for cheap and bought those. I also
found a used 318 oil cooler and purchased that. This seemed to be
going well. I wondered when the trouble would start. No
modification goes this smoothly for me.
My first issue came when I received the steering ram. I have to
say that this was my first experience with modifying a hydraulic system
and I knew next to nothing about hydraulic lines and fittings.
All of the automotive systems I'd done were with factory parts that
just fit. I was in for an education. The ram looked
great. The chrome rod showed no pitting. The fluid that
leaked all over the box it was shipped in was clean and there was no
signs that the ram had been leaking before it was removed. It
came with both hoses, but the fitting on the hoses was not the same as
the fittings on the 318 control valve or lines. I had no clue as
to what I needed to attach the 345 ram to the 318 lines. Over the
course of the next week, I read everything I could find on hydraulic
fittings. I found that the 318 fittings I had were a #6 JIC which
was also known as a 3/8" Army/Navy or AN fitting. The connections
on the 345 ram were of a newer style known as a o-ring face seal or
ORFS. I found some fittings that connected the two, but when I
went to check out, I found I hadn't met the $20 minimum order. I
decided to purchase a hydraulic pressure gauge that I could plug into
the auxiliary fittings on the 317. I had seen one of these listed
as a special tool in my new 317 service CD. Now I needed a
fitting that would plug into the auxiliary hydraulic ports of the 317
and mate up to the 1/4" pipe threads on the gauge. Lost
again. I posed my question
to the Yahoo Deere group, but didn't even receive a reply. I was
on my own - again. I finally learned that the quick connect
hydraulic fittings were
probably made by Parker Hydraulics and the item I needed was a AG
Series (ISO 5675) quick coupler I took a
chance and placed the order. When the parts arrived a few days
later, everything fit. I got lucky again.
I now had my 318
5-port control valve in hand. The first thing on the agenda was
to measure the outside dimensions of the valve body. It was about
3.035" square. This put the center line of the steering shaft at
1.5175". This was 3/8" more than I
wanted. I now had a couple choices. I could either cut out
the 317 steering mount and weld in a new one or I could work with the
existing mount and angle the steering shaft a few degrees to get it to
clear the hole in the dashboard. Decisions, decisions.
By now, Halloween had come and gone and the leaves were beginning to
fall from my trees. I mulched the leaves that had fallen with the
317, then went over them again with the trusty 130. The 130 has
the high lift blades and really does a great job of shredding the
leaves. No raking for this boy. I figured that I'd only
have a few more weeks of mowing before the lawn went to sleep and I
could handle that with the 130. I was looking forward to getting
the 317 into the basement and getting started. I had to pull both
sliding glass doors off the entrance to the basement, but in less than
an hour, the 317 was in the basement and up on jack stands.
With
the
body
off,
it's
time
to
pull
the engine.
It's
even
easier
than
yanking
an
old
VW
bug motor.
Everywhere
I
look,
parts
are
covered
in
dirt.
I wish I would have borrowed a
power washer and cleaned it before moving it into the basement.
The
steering
rock
shaft
is
removed
and
checked
for play. Both
bushings are pretty sloppy, but it won't be used with the power
steering.