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Way Alignment
      Tool
      May 21, 2016
    
Back in 2010
      when I was getting ready to scrape my import mill, I made a crude
      approximation of the King Way alignment tool. It used flat stock
      for the horizontal bar and only used a one vial 6" level that I
      had made using some cast iron and a Starrett 199 - 0.0005" per 12"
      resolution spirit vial. Around the same time, I also made a cross check level
      using two of the Starrett vials, but there was no easy way to
      attach it to the flat bar of the makeshift alignment tool. The
      tool helped with scraping in the mill, but I realized that I
      needed to make another one that was a little closer to the
      original King Way design. I shelved the project for another day.
      Six years later, that day has come. I have a scraping project
      coming up where a proper dovetail way alignment tool would be a
      big help.
    
Over the years,
      I have read a lot about the King Way alignment tool and have
      collected pictures of the King Way and some shop made copies. The
      tool is ingenuously simple. It uses a horizontal bar to hold the
      cross check level, two vertical bars to hold a ground sphere on
      one side and a tube with a slot on the other, and an arm to mount
      a dial test indicator (DTI). In use, the tube with the slot is
      placed on the dovetail or V ways, the ball has a ground ring
      placed beneath it and is positioned on the opposite ways. The
      cross check level is then set to level in both planes and the DTI
      is placed in contact with the way you want to measure for height
      or divergence from parallel. By sliding the tool along the ways,
      you get your readings.
    
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| 
              Squaring up some cast iron blocks. | 
            Cutting
              out some sections to save milling time. | 
          
I started the
      project by squaring up some cast iron blocks on the shaper. I then
      cut and milled the blocks so that holes could be bored at 90° to
      each other. The holes were reamed to 0.501" diameter and then a
      slot was milled with a slitting saw so that the 1/2" diameter
      ground bars could be clamped in the holders.
    
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| 
              Reaming the holes to 0.501". | 
            Progress
              so far. | 
          
The shape of
      each holder was refined a bit and threads were tapped so that the
      clamp could be tightened on the bar. If I had to do the job again,
      I would change the design of the two bar mounts so that the
      mounting point of the horizontal bar would be at the top of the
      mount that supports the vertical bar. This would have allowed me
      to make the level holder a bit shorter.
    
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| 
              Refining the shape. | 
            A
              little more progress | 
          
When the holders
      were finished, I gave them a couple coats of paint using rolled up
      paper to keep the paint out of the reamed holes.
    
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|  Time
              for some paint. | 
            Test
              fitting the tool on the lathe. | 
          
With the two
      holders completed, I set the tool up on my lathe so I could
      measure how wide the holder for the cross check level could be.
      While I wanted to be able to set up the tool on the tailstock ways
      of my small South Bend lathe, the closest I could get the upright
      bars with the level between them was about 3.5". The distance
      between the two inner ways of the SB are about 3.0" center to
      center. This means that I will have to mount the level to the
      outside of the uprights when working on the tailstock ways. I
      could have narrowed the level holder clamp, but I was concerned
      that the weight of the level would rotate on the horizontal bar.
      The original King Way tool gets around this by slotting the
      horizontal bar and using a thumb screw for the level holder that
      locates in the slot. I am using two screws to clamp the holder to
      the bar. So far, it seems to work well.
    
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|  I need
              to measure the distance between the holders and how much
              clearance I have for the cross check level. | 
            Rough
              milling the holder that will attach the cross check level
              to the horizontal bar. | 
          
When I made the
      cross check level, it was machined from a round of cast iron. It
      is 6" x 7.5" x 1.25" thick and it is pretty heavy. I was worried
      that if the T shaped leg of the level was centered on the
      horizontal bar and I used a short tube when testing bed ways, the
      whole tool would tip toward the leg on the long side of the level.
      My solution was to make the level holder able to be reversed and
      thus get the bar clamp closer to the balance point of the level.
      This worked out very well and even with the short 5.5" slotted
      tube, the alignment tool doesn't want to tip when I tried it on
      the lathe. 
    
The level used
      on the King Way tool looks to weigh less than mine. From what I
      understand, it also uses 0.0003" per 12" vials. The bar clamp
      appears to be cast into the level base rather than being an add-on
      piece like my copy.
    
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|  Test
              fitting the holder to the level. The level overhangs the
              holder by a lot on the right side. | 
            I made
              the holder so it could be reversed. This moves the balance
              point a bit to the right. | 
          
Once I had the
      level holder machined and I was able to make sure that it was
      square with the level, I drilled and reamed a 0.501" hole for the
      cross bar. I then machined a slit so that the holder could be
      clamped to the bar. Last, I refined the shape of the holder and
      added a couple pockets in the sides so that the vertical bars of
      the tool could be moved closer together. The upright bars can be
      adjusted to accommodate ways from about 3.5" to 15" apart with the
      current horizontal bar while holding the level between the
      uprights. For checking ways that are closer together than 3.5",
      the level can be moved to sit outside the uprights.
    
When I built the
      cross check level, I ended up making typical vial adjusters after
      a couple of unsuccessful designs. I ended up with coarser threads
      than are generally used for this purpose. My last design used 8-32
      studs and cone shaped nuts that fit into reamed and slightly
      beveled holes on the vial holder end caps. To raise one side of
      the vial, you loosen the top nut, then raise the lower nut, then
      lock the top nut back down. This was a little fiddly because the
      8-32 threads lift and lower the vial more than the resolution of
      the vials with barely a fraction of a turn. It took some of time
      to get the level adjusted, but once it was adjusted, it seemed to
      stay put pretty well. After more than a year of storage, the
      bubbles still centered perfectly. Now that I was using the level
      on the alignment tool, I needed to be able to re-level the vials
      with each use of the tool. I also wanted the ability to adjust the
      vials more finely. To do this, I decided on using a differential
        screw adjuster on one side of the vial holder. I had a spare
      brass end cap I had made when I built the brass vial holders. For
      a proof of concept, I tapped this end cap for 1/4"-20 threads. For
      the adjuster, I used a 1/4"-20 bolt with 8-32 internal threads
      tapped in to fit on to the 8-32 studs. This allowed me to raise or
      lower one end the vial holder by 0.01875" per revolution of the
      bolt. Not a fine enough adjustment for the sensitivity of the
      0.0005" per 12" resolution vials, but better than the 8-32 threads
      alone. The test worked out very well. I found that I could adjust
      the vial pretty easily.
    
To make the permanent adjusters, I ordered some 1/4"-28 threaded studs and a 1/4"-28 tap. The closer the thread count of the differential screws are to each other, the finer the adjustment. The 1/4"-28 and the internal 8-32 threads would give me 0.0045" height adjustment for every revolution of the adjuster. A tenth of a revolution on the adjuster would raise or lower the vial holder by about half a thousandth. Not a super-fine adjustment, but it should be sufficient. I turned and knurled some adjustment thumb screws from brass to top off the adjustment screws. To get both gross and fine adjustments, I turned an 8-32 adjuster for one side of the vial and use the differential screw on the other. One side for gross adjustment and the other side for fine adjustment. Though they're not shown in the picture below right, I ended up putting springs under each side of the vial holder end caps to help hold the vials to their adjustment. I have to say that the adjusters turned out to work as well as I had hoped they would. It is very easy to get the level into adjustment as long as I have the cross bar somewhat level.
I made up a new
      slotted tube from the only appropriately sized stock I had on
      hand, 1" schedule 40 steel pipe. I need to purchase some tube with
      a 1/4" wall thickness to make the proper part, but decided that
      making a slotted tube from the schedule 40 pipe would give me a
      chance to play with the tool and get some practice using it. I
      also need to find my shop made tool post grinder to grind the end
      diameters of the next tube I make. I haven't come across it since
      we moved into the new house and shop, but I still haven't unpacked
      all of the boxes yet. 
    
In the last two
      pictures, the new slotted tube has been machined. The center
      section of the slot in the tube has been relieved so that only the
      1" sections at each end contact the ways. To get the mating
      surfaces of the ends of the tubes square with the ways, I put a
      coat of ink from a felt tipped marker on the four flats, then
      rubbed the tube against both some V and dovetail ways. I used a
      fine file on the area where the ink had been rubbed off until I
      had four surfaces that contacted flush with the ways. The process
      was very similar to scraping flat surfaces, only I used a file
      instead of a scraper. Before I aligned the tube's slot, I tapped
      four holes into the tube. Two for V ways and two for dovetail.
      Because the pipe is so thin, I didn't get much thread engagement
      for the 1/2"-13 threads I turned on the ground 1/2" O1 stock , but
      it will have to do until I get the proper thick walled tube. The
      extra hole for each position will allow me some choice in
      positioning the slotted tube to see what works best.
    
With the tool
      more or less complete, I set it up on my SB9 lathe to test it out.
      Since the tailstock ways on the workshop lathe are only about 3"
      apart, I needed to move the level to outside the uprights. Since
      this puts the weight of the level to one side, I needed to
      counter-weight the horizontal bar to keep the tool from tipping.
      Not the best procedure, but it seems to work OK.
    
For my test of
      the new tool, I will attempt to measure the wear of the saddle
      ways on my lathe. It should be good practice for the upcoming
      project. To make sure that I am getting true readings, I will
      first check and correct for any twist in the lathe bed. The
      tailstock ways are realatively unworn. The scraping that was done
      at the factory to dust off the planer marks when the ways were
      machined are still evident, so using the tailstock ways to check
      for twist should be pretty accurate. In the past, I have attempted
      to correct for any twist by turning collars on a long piece of
      stock, then shim the lathe bed until I was able to turn the
      collars to pretty close to the same diameter. I currently have a
      0.002" shim on the operator's side of the lathe bed foot at the
      tailstock end. However, as some sage person once said, "Machine
      tools are made of rubber." Add the fact that this light lathe is
      mounted to a butcher block bench and there is no doubt that the
      twist of the bed could change with the seasons. I am looking
      forward to seeing how close I can get the lathe to being free of
      twist and then checking the lathe for wear.
    
Using the setup
      shown in the last two pictures, using no DTI and just reading the
      level bubbles, I checked the tailstock ways for twist. The
      readings I got made me scratch my head. With both vial bubbles
      centered at the headstock end, I moved the tool to the right about
      six inches. The bubble measuring the X axis, the direction that
      the top slide moves, showed three increments high on the flat way
      side. I slid it toward the tailstock another six inches. It was
      now showing two increments high. At the third six inch stop, or
      18" from the headstock, the bubble was centered again. The vial
      for the Z axis, left to right along the ways, showed the bubble
      pretty close to centered at each stop. I set up the DTI to measure
      the outer angled flat of the front V way and repeated the test.
      The V way showed less than 0.0003" deviation over the 18". It
      showed a little wear about 6" from the spindle snout and 0 in
      front of the snout and after about 12" from the snout.
    
Apparently I
      have a hump in the ways closest to the operator. Three divisions
      of the Starrett 199 vials would be 0.0015" per 12". That seemed
      like a lot. I quit for the night and decided to give it some more
      thought. The next day, I repeated the test with the same results
      and then it dawned on me that I was using vials calibrated to
      measure 12" and I was actually measuring the rate of slope for
      ways 3" apart. Duh. So the hump is there, but it's not 0.0015",
      it's closer to 0.00035". To confirm my thoughts, I re-leveled my
      surface plate using my frame level (0.0002" per 10") and used a
      0.100" and a 0.10025" gauge block under my best wide parallel with
      the frame level above it. The results from placing the gauge
      blocks 12" apart and 3" apart and measuring their respective
      slopes confirmed my thoughts. Sometimes I need to spend the extra
      time to confirm what I think I know.
    
I will have to
      remember that the distance between the slotted tube and the sphere
      determines the amount of rise or fall that is depicted by each
      increment on the spirit vial. As for the South Bend, while I would
      prefer no hump in the ways, 3 1/2 ten-thousandths is a lot better
      than a thousandth and a half. I doubt that I will do anything to
      try and correct this. I have learned to produce pretty accurate
      work on this lathe in spite any deficiencies it may have. 
      Knowing where it is inaccurate will help me to produce better
      work.
    
I have a couple
      old lathe beds that I will spend some time mapping out. I need
      some practice time with this tool before I start using it to help
      me scrape ways that are true.
      
    
© Fager May 21, 2016